1998 Toyota 4runner Engine Problems
15 owner-reported engine complaints from NHTSA data
Data sourced from NHTSA public database. For informational purposes only. Always consult a qualified mechanic.
Owner Complaints (15)
TL*THE CONTACT OWNS A 1998 TOYOTA 4RUNNER. DURING DECELERATION, THE VEHICLE STALLS AND ACCELERATES BOTH AT THE SAME TIME. THE DEALER REPLACED THE IDLE SWITCH VALVE TWICE, WHICH CORRECTED THE FAILURE FOR A FEW MONTHS. ON AUGUST 21, 2008 WHILE DRIVING 40 MPH, THE VEHICLE SHUT DOWN. THE CONTACT WILL TAKE THE VEHICLE TO THE DEALER FOR A DIAGNOSIS. THE FAILURE MILEAGE WAS 72,100 AND CURRENT MILEAGE WAS 90,000.
I WAS DRIVING ON HWY. 45 ABOUT 65 MPH. MY SISTER AND NEPHEW WERE IN THE VEHICLE WITH ME. ALL OF A SUDDEN, WE HEARD A LOUD POP. I FELT THE POWER GO OUT OF THE VEHICLE AND PROCEEDED TO PULL OVER TO THE SHOULDER OF THE FREEWAY - ALMOST HITTING ANOTHER VEHICLE. MY NEPHEW SAID IT SOUNDED LIKE WE GOT A FLAT TIRE. THEN WE NOTICED SMOKE COMING OUT FROM UNDER THE HOOD OF THE VEHICLE. WHEN WE GO TOUT, WE NOTICED OIL ON THE GROUND -UNDER THE VEHICLE. WE LIFTED THE HOOD - AND NOTICED A HOLE IN THE ENGINE BLOCK. THE VEHICLE HAD TO BE TOWED TO A GAS STATION, AND THEN PICKED UP THE NEXT DAY BY THE REPAIR SHOP. THE VEHICLE IS UNDER WARRANTY WITH GAP INSURANCE. THE REPAIR SHOP IS TELLING ME THE WARRANTY DOES NOT COVER IT, AND THAT IT IS NOT A MANUFACTURE MALFUNCTION. I ALSO HAD JUST WITHIN LESS THAN A MONTH AGO, HAD TO HAVE THE STARTER REPLACED, PRIOR TO THIS HAPPENING.
WITH 50 000 MILES, CONNECTING ROD BROKE WHILE DURING NORMAL USE, SHOT OUT THE ENGINE BLOCK, FLUID SPILLED, ENGINE SEIZED AND CATASTROPHIC DAMAGE TO ENGINE BLOCK; NEW ENGINE REQUIRED. *JB
WE WERE ON VACATION DRIVING FROM ATLANTA, GA TO DAMARISCOTTA, ME. ON THE MORNING OF SATURDAY AUGUST 7, WE BEGAN OUR SECOND DAY OF TRAVEL JUST OUTSIDE OF HARRISBURG, PA. WE WERE ENTERING THE INTERSTATE WHEN WE HEARD A LOUD POP AND THE CAR BEGAN TO SHAKE BADLY. WE IMMEDIATELY TOOK THE CAR, A 1998 TOYOTA 4RUNNER WITH FEWER THAN 60,000 MILES ON IT, TO HARRISBURG TOYOTA. THE DEALER EVENTUALLY TOLD US WE HAD A BROKEN ROD AND NEED A SHORT BLOCK REPLACEMENT, FOR WHICH WE WERE CHARGED $5500, INCLUDING $3900 IN PARTS.*AK
CONSUMER STATED WHILE TRAVELING AT ANY SPEED AND WITHOUT ANY INDICATION VEHICLE WOULD STALL. VEHICLE WAS SERVICED, TECHNICIAN NOTICED A MOUSE HAD CRAWLED INTO THE MASS AIR FLOW . *AK
THERE WAS AN UNFAMILIAR RATTLING NOISE COMING FROM THE ENGINE. *DT *JB
WHILE DRIVING THE VEHICLE WAS LEAKING EXHAUST FUMES INSIDE THE VEHICLE. DEALER HAS BEEN NOTIFIED. PLEASE PROVIDE FURTHER INFORMATION. TS
CONSUMER STATED THAT THE CHECK ENGINE LIGHT CAME ON DUE TO OXYGEN SENSOR FAILURE. *YH
WHILE CONSUMER WAS DRIVING ON A MOUNTAIN/COMING DOWN AND EXITING, VEHICLE COMPLETELY SHUTDOWN, THIS HAS HAPPENED TWICE. CONSUMER WAS TOLD BY DEALER THAT VEHICLE WAS FINE. IT JUST NEEDS TO GET USED TO MOUNTAIN DRIVINGB (NOTE: THE VEHICLE HAS A SUPERCHARGER THAT THE DEALER ADDED WHEN THE VEHICLE WAS NEW, ITS A TRD SUPERCHARGER). *AK *YH
WHILE ACCELERATING 55 MPH ENGINE SEIZED UP, LOSING COMPLETE POWER. OWNER DRIFTED TRUCK OVER TO THE SIDE OF THE ROAD. DEALERSHIP STATED THAT ENGINE THREW A ROD. PLEASE DESCRIBE DETAILS. *AK
THE VEHICLE WAS GOING 15MPH ON WET PAVEMENT AND SUDDENLY BROKE INTO A 360 SPIN. THE ENGINE STALLED CAUSING THE VEHICLE TO LOSE ALL POWER, LOCKING THE BRAKES UP. THE DEALER WAS NOTIFIED. NLM *TT
WHILE DRIVING 20 MPH VEHICLE BEGAN TO LOSE POWER, ENGINE CONTINUED TO RUN, AND THE INSTRUCTMENT PANEL LIGHTS REMAINED ILLUMINATED. CAUSE UNKNOWN. PLEASE GIVE ANY FURTHER DETAILS. *AK
VEHICLE EXPERIENCING ENGINE KNOCKING AND STALLING. YH
ENGINE STALLS WHILE DRIVING ,LOSS OF ENGINE POWER. DEALER CANNOT DETERMINE DEFECT. *AK
VEHICLE IN HEAD ON COLLISION, FIRE ERRUPTED IMMEDIATELY. (QCAW)