2006 Kia Sorento Engine Problems
54 owner-reported engine complaints from NHTSA data
Data sourced from NHTSA public database. For informational purposes only. Always consult a qualified mechanic.
Owner Complaints (54)
Your 2006 Kia Sorento caught fire while parked and turned off. The fire department extinguished it, but the exact cause couldn't be determined. An independent mechanic declared the vehicle a total loss due to the fire damage.
Parts you may need:
As an Amazon Associate, MyCarTSB earns from qualifying purchases.
While driving, your engine suddenly began to shake and rattle violently before the car stalled. The dealer diagnosed that the crankshaft bolt and crankshaft pulley had failed. Both the crankshaft pulley pin and crankshaft bolt were replaced to fix the problem. The fix involves removing and replacing these engine timing components.
Parts you may need:
As an Amazon Associate, MyCarTSB earns from qualifying purchases.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. WHILE DRIVING 40 MPH, THERE WAS AN ABNORMAL SOUND COMING FROM THE ENGINE COMPARTMENT. THE CONTACT STATED THAT THE BRAKE, CHECK ENGINE, AND BATTERY WARNING INDICATORS ILLUMINATED. ALSO, THE VEHICLE BECAME DIFFICULT TO STEER. THE VEHICLE WAS TOWED TO AN INDEPENDENT DEALER WHERE IT WAS DIAGNOSED THAT THE CRANK SHAFT PULLEY BOLTS FRACTURED, WHICH CAUSED THE PULLEY AND THE SERPENTINE BELTS TO SEPARATE FROM THE ENGINE. THE MECHANIC WAS UNABLE TO REPAIR THE VEHICLE AND THE VEHICLE WAS TOWED TO ARAPAHOE KIA (9701 E ARAPAHOE RD, CENTENNIAL, CO 80112, (888) 236-7975). THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 111,000. *TT *TR
TL* THE CONTACT OWNED A 2006 KIA SORENTO. WHILE DRIVING 35 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS UNABLE TO RESTART THE VEHICLE. THE CONTACT WAS INFORMED BY A PASSING MOTORIST THAT THE VEHICLE WAS ON FIRE. THE FIRE DEPARTMENT WAS NOTIFIED AND WAS ABLE TO EXTINGUISH THE FIRE. THERE WERE NO INJURIES AND NO REPORTS WERE FILED. THE VEHICLE WAS DESTROYED AND REMAINED AT THE SCENE OF THE FIRE. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 120,000. THE VIN WAS NOT AVAILABLE.
BOUGHT CAR STARTED HAVING AN OVER HEATING PROBLEM. COMPRESSION TEST CAME BACK WITH COMPLETE PASS NOTHING ABNORMAL. CAR WAS NOT STARTING WITHOUT A JUMP SO BOUGHT A NEW BATTERY FOR IT EVERYTHING SEEMED COMPLETELY FINE. DROVE A TOTAL OF MAYBE TEN MILES TO ACE HARDWARE TO GET SOME SUPPLIES AND CAR STARTED TO SMOKE ONCE I TURNED THE HEATER OFF.IMMEDIATELY PULLED OVER WHITE SMOKE COMING FROM UNDER HOOD, PUDDLE OF FLUID IN PARKING SPOT, AND WATER BOILING SOUND UNDER HOOD. TOWED CAR HOME THEN TO MECHANIC WHERE IT IS SITTING NOW FOR AN ESTIMATE BEING TOLD IT LOOKS LIKE I WILL NEED A NEW MOTOR. THERE IS 106,661 PLUS OR MINUS A 100MILES I AM THE SECOND OWNER OF THE WELL MAINTAINED VEHICLE.WHEN SMOKING STARTED I WAS DRYING ON A HWY WITH SPEED LIMIT OF 55 MILES/HR. IT IS AN AWD PASSED SMOG, AND I BOUGHT IT FROM A DEALER WHO BOUGHT IT FROM AN AUCTION. IT WAS A TRADE IN BY LESSEE TO THE LESSOR FOR A NEWER ONE. *TR
THIS IS THE THIRD TIME THAT THIS HAS HAPPEN TO ME. I WAS DRIVING AND MY CAR STOP IN THE MIDDLE OF THE STREET NEED A TOW TRUCK SO I TOOK IT TO THE SHOP AND THE DIAGNOSE WAS CRANK SHIFT SENSOR $700.00. ABOUT 3 YRS LATER DRIVING ON THE FREEWAY LOST ALL POWER LIGHT CAME ON GUIDE OF THE FREEWAY I TOOK IT TO THE SHOP THE SAME PROBLEM AGAIN CRANK SHIFT SENSOR AGAIN $700.00. THE YR DRIVING FROM WORK ON THE FREEWAY IT HAPPEN AGAIN NO POWER LIGHT CAME ON ANOTHER $ 700.00. [XXX]. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR
WHILE MOVING AT 70 MPH INTERSTATE SPEED LIMIT, MY DAUGHTER HEARD A LOUD POP AND THE ENGINE MADE POPPING NOISES AS SHE BROUGHT THE SUV TO A STOP ON THE SIDE OF THE INTERSTATE. SHE ULTIMATELY RESTARTED THE VEHICLE AND DROVE AT 30 MPH WITH FLASHING HAZARD LIGHTS ON UNTIL REACHING THE NEXT EXIT (2-3 MILES MAX.) TO A SAFE LOCATION BEING AROUND 9:00 PM IN THE EVENING. THE SUV WAS TAKEN TO A FIRESTONE MASTERCARE STORE IN CHATTANOOGA, TN. AFTER REMOVING THE ENGINE COVER, THE MECHANIC FOUND PART OF THE SPARK PLUG AND IGNITION PART, INDICATED THAT THE LOCATION WHERE THE SPARK PLUG WAS INSERTED HAD BEEN STRIPPED OUT BY THE PARTS BLOWING OUT OF THEIR NORMAL LOCATION WITH EXTREME PRESSURE. THE SUV HAS BEEN TOWED TO MY HOME WHERE IT IS SITTING PENDING WHAT OPTIONS ARE AVAILABLE FOR REPAIR.
BELT SPROCKET AND HARMONIC BALANCER WITH BOLT. THE BOLT IS MADE OF SUBSTANDARD MATERIAL AND BROKE CAUSING THE AUTOMOBILE TO LOSE POWER STEERING AND OTHER VITAL CAR FEATURES. NO WARNING, IT JUST BROKE WHILE IN MOTION CAUSING ALL OF THE BELTS TO SEIZE. I WAS ON A HILLY MOUNTAINOUS ROAD IN MY HOME AREA OF HIGH RIDGE MISSOURI, ACUTALLY ON THE HIGH RIDGE.I AM LUCKY THAT I AM SMART ENOUGH TO DRIVE DEFENSIVELY AND WAS ABLE TO COAST TO A SAFE SIDE ROAD. TWO MECHANICS CAME TO MY RESCUE AND EASILY SAW THAT THE PROBLEM STATING THAT I WOULD NEED A WHOLE NEW ENGINE.I HAVE A TEMPORARY FIX ESTIMATE FROM MY MECHANIC BUT HE SAYS THE CAR REALLY NEEDS A WHOLE NEW ENGINE.....
6/2015 VEHICLE BEGAN TO RUN ROUGH. LOCAL MECHANIC DISCOVERED CRANKCASE BOLT HAD SNAPPED AND THE PULLEY AND BALANCER MOUNTING SCREW HAD SHEARED OFF. SHOP CONFIRMED A KIA KIT TO FIX THE ISSUE ($1200.00 + 1007.00 FOR TIMING GEAR KIT AND WATER PUMP) 1/15/2016 WHILE DRIVING INTO THE ROUNDABOUT ON PORTAL WAY (15 MPH) THERE WAS A LOUD CLUNK FROM THE ENGINE COMPARTMENT IMMEDIATELY FOLLOWED BY THE LOSS OF POWER STEERING, ASB BRAKING AND VOLTMETER WARNING LIGHTS. THE VEHICLE WAS TOWED TO MECHANICS SHOP WHERE IT WAS CONFIRMED THAT THE NEW CRANKCASE BOLT HAS BROKEN AGAIN DAMAGING THE NEW PULLEY AND BALANCER ALSO. THE SHOP CONTACTED THE LOCAL KIA DEALER AND THEY CONFIRMED THAT THE 2003-2006 V6 3.5L MISABISHI ENGINES USED HAVE A LONG RECORD OF THIS PROBLEM WITH NO PERMANENT FIX. THE FOLLOWING INFORMATION WAS EMAILED TO ME FROM THE OWNER OF AXTON AUTOMOTIVE, FERNDALE WA AN ASE CERTIFIED SHOP, "ON WEDNESDAY, JANUARY 20, 2016, AXTON AUTOMOTIVE <AXTONAUTOMOTIVE@GMAIL.COM> WROTE: HELLO, ON YOU KIA. IT DOESN'T LOOK LIKE ANY FIX IS PERMANENT ON THE VEHICLE. EVEN THEIR OWN RECALL/FIX IS FAILING. I RECOMMEND FILING A COMPLAINT AT THE NATIONAL HIGHWAY TRAFFIC SAFETY ADMINISTRATION.. I WILL COME UP WITH SOME OPTIONS TOMORROW AND GET BACK TO YOU. BUT WHATEVER WE DECIDE I RECOMMEND NOT USING THIS VEHICLE. JIM" THE VEHICLE IS DISABLED AT THIS TIME WITH NO RESPONSE FROM KIA.
KIA SORENTO - I HAVE A 2006 SORENTO THAT JUST TURNED 60,000 MILES IN OCTOBER. I HAD DRIVEN IT AT LUNCH ONE DAY, WHEN I WENT TO LEAVE THE OFFICE AT 5, THE CAR WAS MAKING AN AWFUL GRINDING NOISE AND THE EMERGENCY BRAKE LIGHT CAME ON, EVEN THOUGH THE BRAKE WAS NOT ON. THEN THE POWER STEERING WENT OUT. I HAD TO HAVE IT TOWED IN BECAUSE THE CRANKSHAFT MALFUNCTIONED AND THAT ALONG WITH ALL THE BELTS AND PARTS HAD TO BE REPLACED. IT TOOK 5 WEEKS FOR THE REPAIR, AND NOW IT HAS TO GO BACK BECAUSE ONE OF THE NEW BELTS IS SCREECHING. I PAID $1,300 FOR THE REPAIR AND KIA ONLY PAID PART OF THE REPAIR. WHY WOULD THEY PAY FOR PART AND NOT ALL, IF IT WAS A DEFECTIVE PART THAT THERE SHOULD HAVE BEEN A RECALL ON?
TL* THE CONTACT OWNS A 2006 KIA SORENTO. WHILE DRIVING AT APPROXIMATELY 30 MPH, THE ENGINE STALLED AND ALL THE WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS TOWED TO A DEALER WHERE IT WAS DIAGNOSED THAT THE CRANK SHAFT PULLEY BOLT FRACTURED AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 83,000. THE VIN WAS UNAVAILABLE.
2006 KIA SORENTO. CONSUMER WRITES IN REGARDS TO DESIGN DEFECT WITH THE ENGINE CRANKSHAFT SPROCKET. CONSUMER HAS PREVIOUS CORRESPONDENCE WITH DIFFERENT ODI# (NAR) AND ISSUE IN ARTEMIS. *SMD THE CONSUMER STATE IF THE BOLT BREAKS, THE ENGINE WILL STALL AND POWER STEERING WILL BE LOST. *JB
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT WHILE DRIVING AT 60 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS UNABLE TO RESTART THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE CRANK POSITION SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 225,000.
WHILE DRIVING DOWN HIGHWAY, BOTH THE BREAK LIGHT AND BATTERY LIGHT CAME ON AND LOST POWER STEERING. WAS ABLE TO MAKE IT TO A SAFE LOCATION. WHEN AT FIRST GLANCE IT APPEARED THAT THE MAIN BELT HAS SLIPPED OFF THE PULLEY. WHEN TOWED TO A SERVICE STATION FOR ASSESSMENT AND REPAIR, IT WAS DISCOVERED THAT THE HARMONIC BALANCER BOLT HAD BROKEN OFF IN THE CRANKSHAFT. WE ARE STILL IN PROCESS OF TRYING TO FIND OUT OF THE REMAINING PART OF THE BOLT CAN BE REMOVED OR IF THE ENTIRE ENGINE WILL NEED TO BE REPLACED. THE BOLT IS NOT CONSIDERED A 'WORKING PART' OF THE ENGINE AND EXTENDED WARRANTY REFUSES TO COVER THE REPAIRS. THE ROOT OF THE PROBLEM IS IN THE ROLL PIN INSIDE THE CASING THAT WEARS DOWN AND THE BOLT CAN NOT SUPPORT THE STRESS. KIA HAS HAD A RECALL ON MODEL YEARS 2003 AND 2004 BUT THE PROBLEM CONTINUES FOR 2005 AND 2006 YEARS AND RESEARCH IS SHOWING THAT KIA IS NOT COVERING THE PROBLEM FOR 2005 OR 2006
TL* THE CONTACT OWNS A 2006 KIA SORENTO. WHILE DRIVING APPROXIMATELY 65 MPH, THERE WAS AN ABNORMAL NOISE COMING FROM THE HOOD OF THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE HARMONIC BALANCE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 119,000.
WHILE DRIVING ALMOST HOME, (2-MILES) THE POWER STEERING STOPPED, WE PULLED INTO A GAS STATION, BARELY MISSING THE FUEL PUMPS. THE BELT CAME OFF. WHEN THE MECHANIC ASSESSED THE PROBLEM, IT WAS MUCH GREATER. THE HARMONIC BALANCER WAS LOOSE, AND THE DRIVE PIN TO THE CAM BELT GEAR HAD SHEERED OFF. THE REPAIRS WERE COSTLY $1300.00. THIS IS A DESIGN DEFECT AND HAS AFFECTED THOUSANDS OF KIA OWNERS. THE OWNERS ARE LIKE MYSELF AND DON'T KNOW WHAT TO DO, SO WE JUST PAY THE BILL.. KIA DENIES ANY ISSUES. THIS A HUGE KIA COVER UP! IT HAS BEEN A KNOWN DEFECT FOR A LONG TIME, AND KIA DOES NOT WANT TO PAY FOR ALL THE DAMAGES, AND I'M SURE THE ACCIDENTS.
WENT TO LEAVE HOUSE VEHICLE STARTED. FELT LIKE BRAKES WERE LOCKED LOOKED AT DASH RED LIGHTS FOR CHECK ENGINE AND BRAKE LIGHT WAS ON. ENGINE WAS RUNNING POPPED THE HOOD SEEN FAN BELT WASN'T TURNING. CALLED AAA
STARTED MAKING LOUD KNOCKING NOISE TOOK TO REPAIR SHOP TO FIND OUT THE PROBLEM IS WITH THE CRANKSHAFT BOLT, AS MANY OTHER KIA OWNERS HAVE BEEN HAVING. *TR
WAS SITTING PARKED THANKFULLY BUT THE CRANKSHAFT BOLT SHEARED OFF CAUSING LOSS OF POWER STEERING AND LOSS OF ALTERNATOR. THIS IS THE SECOND TIME THIS HAS HAPPENED WITHIN A YEAR. THANKFULLY WE WEREN'T IN MOTION WHEN THIS HAPPENED. PLEASE INVESTIGATE AS THIS KEEPS HAPPENING AND HAS HAPPENED TO A LOT OF KIA SORENTO OWNERS (LOOKING ONLINE). KIA ISSUED A SERVICE MEMO TELLING THE SERVICE PEOPLE TO USE AN UPGRADED BOLT, HOWEVER WE HAD THE UPGRADED BOLT AND THE ISSUE STILL OCCURRED. *TR
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT THE VEHICLE FAILED TO START. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE CRANK SHAFT BOLT FRACTURED AS A RESULT THE ENGINE AND CRANK SHAFT BOLT NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 138,000.
MY 2006 KIA SORENTO, MANUFACTURED IN AUGUST 2005 & WAS A BASIC VEHICLE, NO LUXURY MODEL.A RENTAL CAR BUSINESS WAS 1ST OWNER AND ONLY HAD IT FOR A FEW MONTHS, THEN I BOUGHT IT FROM A DEALER IN SEPT 2006 W 14,000 MILES. IT IS 8 YEARS OLD WITH 108,000 MILES. THE CHECK ENGINE LIGHT TURNED ON, I HEARD LOUD BANGING IN THE HOOD, THEN SUDDENLY IT TURNED OFF WHILE I WAS DRIVING ON CITY STREETS. TRAFFIC WAS SLOW MOVING. I HAD IT TOWED TO AN EXPERT MECHANIC AND OWNER OF HIS OWN SHOP. MY MECHANIC HAS DONE SOME PREVENTIVE MAINTENANCE IN THE PAST AND CONSIDERED IT TO BE IN EXCELLENT CONDITION. HE TOOK THE ENGINE APART AND FOUND PIECES BROKEN OFF FROM THE "INTAKE RUNNER BUTTERFLY VALVE ASSEMBLY & FELL INTO THE ENGINE; ALSO THERE WAS A BUSHING FAILURE IN THE LOWER INDUCTION MANIFOLD. MY 3.5 ENGINE WAS TOTALED WITHIN MINUTES ALONG WITH ALL SURROUNDING PARTS. THE SAME ENGINE AS IN THE RECALL. MY KIA HAS A 3.5 ENGINE, SAME AS IN THE RECALL BULLETIN #TT2008020601. THE RECALL BULLETIN WAS FOR KIA MODELS 2003-2005, YET THIS EXACT INCIDENT WAS DESCRIBED IN THE RECALL BULLETIN. I HAVE TWO PHOTOS OF SOME OF THE DAMAGE (1ST PHOTO IS THE INTAKE RUNNER ASSEMBLY W/TWO BROKEN MISSING BUTTERFLIES FOR CYLINDERS 5 & 6 & THE 2ND PHOTO OF A PIECE OF THE BUTTERFLY STUCK IN THE INTAKE PORT OF THE CYLINDER HEAD -BOTH TAKEN ON 9-12-2014.) I THEN HAD IT TOWED TO A GARDEN GROVE KIA DEALERSHIP. THEY INSPECTED & GAVE ME AN ESTIMATE OF $11,700. ALL THEY SAID IT WAS OUT OF WARRANTY AND THAT 2006 MODELS WAS NOT PART OF THE RECALL. HOW CAN KIA CORPORATION GUARANTEE THAT THE SAME INFERIOR PARTS WERE NOT INSTALLED IN MY 2006 SORENTO? IT WAS MANUFACTURED IN 2005. KIA CORPORATION SHOULD TAKE RESPONSIBILITY FOR THE DAMAGE DUE TO THE FACT THAT THIS PROBLEM WAS NOT COMPLETELY RESOLVED WITH THE 2005 MODELS. *TR
CAR AT FIRST WOULD SHUT OFF WHILE DRIVING , PULLED CAR OVER AND WOULD START BACK UP, TOOK CAR TO MECHANIC AND SAID IT WAS THE CRANKSHAFT SENSOR, REPLACE CRANK SHAFT SENSOR, FEW WEEKS LATER PROBLEM RETURN, MECHANIC THOUGHT IT WAS THE CAMSHAFT SENSOR STILL HAD THE PROBLEM OF CAR SHUTTING OFF WHILE DRIVING IN CITY AND HIGHWAY.FINALLY AFTER MONTHS OF BACK IN AND OUT OF THE MECHANICS WHILE DRIVING CRANKSHAFT BOLT BROKE WHILE DRIVING, AFFECTING THE HARMONICA BALANCER AND TIMING BELT CAUSING THE VEHICLE TO LOSE ALL POWER IN THE CAR AND HAD NO POWER STEERING, VERY LITTLE CONTROL OF THE VEHICLE, COASTED INTO DRIVEWAY LUCKILY NO ON-COMING CARS , AFTER SPENDING SEVERAL HUNDREDS OF DOLLARS FOR REPAIRS, MECHANIC IS TELLING ME THE ENGINE IS NO GOOD, CAR IS UNDRIVABLE NEEDS NEW ENGINE AT COST OF 5300 DOLLARS. *TR
I HAVE A 2006 KIA SORENTO. MY 16 YEAR OLD DAUGHTER WAS DRIVING HER BROTHERS TO PRACTICE AND THE CAR TOTALLY LOCKED UP, THE ENGINE FAILED, SHE HAD LOSS OF THE POWER STEERING, LOSS OF THE COOLING SYSTEM, ALL TOGETHER LOSS OF CONTROL OF THE VEHICLE WHILE SHE WAS DRIVING AND FORTUNATELY, FOR US, SHE WAS ABLE TO GET IT OFF THE ROAD SAFELY. THIS WAS AN EXTREMELY HAZARDOUS CONDITION NOT ONLY TO HER AND HER BROTHERS BUT TO OTHER DRIVERS ON THE ROAD AND THAT WERE AROUND. WE HAD THE CAR TOWED TO A MECHANIC AND HE SAID THE BOLT SHEARED OFF IN THE ENGINE AND HE COULD NOT GET TO IT AND THE WHOLE ENGINE WOULD NEED TO BE REPLACED. HE SUGGESTED WE TOW IT TO THE LOCAL KIA MECHANICS. AFTER HAVING IT TOWED TO THE KIA DEALERSHIP, IT WAS CONFIRMED THAT THE CRANKSHAFT BOLT SHEARED OFF CAUSING DAMAGE. I WAS FURTHER TOLD THIS HAS BEEN A RECURRING ISSUE WITH KIA SORENTOS AND THERE WAS EVEN A RECALL ON THIS EXTREMELY DANGEROUS ISSUE. THE DEALERSHIP TELLS ME MY CAR IS NOT INCLUDED IN THE RECALL. I AM AT A COMPLETE LOSS AS TO HOW THIS IS AN ON GOING DOCUMENTED PROBLEM WITH THE BOLT IN MODELS JUST PRIOR TO MY SORENTO BEING RECALLED AND THE SAME ISSUE EXISTING IN MY VEHICLE AND IT IS NOT INCLUDED WHEN IT IS QUITE OBVIOUS THAT THE PROBLEM IS THE SAME. NOT ONLY DID THEY PUT MY CHILDREN IN A DANGEROUS SITUATION BY NOT DISCLOSING OR PROVIDING SOME SOLUTION TO A PROBLEM THAT THEY ARE WELL AWARE OF AND IS DOCUMENTED, THEY HAVE NOW CAUSED EXTREME DISTRESS. THERE IS A FLAW IN THE MANUFACTURING OF THEIR VEHICLES AND AN OBVIOUS BREAKDOWN IN THEIR RECALL PROCESS AND AS A RESULT THEIR CUSTOMERS ARE SUFFERING! THIS IS A SAFETY ISSUE THAT SHOULD BE RESOLVED QUICKLY. THANK GOODNESS NO ONE WAS HURT, THIS TIME! THESE ARE PEOPLE'S LIVES THAT THEY ARE PUTTING AT RISK DAILY! *TR
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STARTED THE VEHICLE AND HEARD A STRANGE NOISE. HE PROCEEDED TO DRIVE THE VEHICLE AND IT STALLED AT 30 MPH. THE INSTRUMENT PANEL INDICATORS ILLUMINATED. THE DEALER STATED THAT THE CRANKSHAFT PULLEY BECAME LOOSE AND THE BOLT WAS FRACTURED. THE VEHICLE WAS NOT REPAIRED AND THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS 75,000.
25 MINUTE DRIVE TO TOWN. SQUEALING SOUND. PULLED OVER, THE CRANK SHAFT PULLEY WAS SO LOOSE THAT THE BOLT COULD BE HAND TIGHTENED. MECHANIC SAID PIN FELL OUT AND BOLT SHEERED. MAY NEED NEW ENGINE. COULD HAVE DESTROYED THE CRANK SHAFT. ALSO HAVE TRANSMISSION HESITATION, THE 4X4 LOW LIGHT ON DASH GOES ON AND THE TRANSMISSION KICKS IN LOW . HAVE TO SIT AND WAIT FOR IT TO GO OFF. THIS HAPPENS WITH OUT THE BUTTON BEING TURNED ON. THIS KIA ONLY HAS 79,000 HIGHWAY MILES. ITS AMESS. THIS CRANK SHAFT HARMONIC BALANCER SHOULD LAST THE LIFE OFF THE VEHICLE. SOME ONE IS GOING TO DIE OR GET SERIOUSLY INJURED BECAUSE WHEN THIS HAPPENED YOU COULD NOT STEER THE KIA OR USE BRAKES. *TR
WITH ONLY 46000 MILES, I HEARD A SOUND, AND LIKE EVERYONE ELSE WHO HAS POSTED THIS PROBLEM, NO POWER STEERING, EVERYTHING LITE UP ON DASH PANEL. THE CRANK SHAFT PULLEY BOLT WAS BROKEN. I WAS ABLE TO GET IT TO A MECHANIC, HE REPLACED THE BOLT. THEN 3 DAYS AGO, THE SAME THING!!! I HAVE HAD PROBLEMS WITH THE BREAK LIGHTS BURNING OUT AT LEAST EVERY 3 MONTHS-CLOCK CHANGES TIME. THREE YEARS AGO THE AIR CONDITION FAILED, AFTER MUCH DEBATE, KIA FIXED IT. HOW CAN THIS NOT BE A RECALL?! IF I CAN GET THIS FIXED-NEVER WILL I BUY OR RECOMMEND A KIA OF ANY KIND!!!!! *TR
I WAS DRIVING DOWN THE STREET IN MY KIA SORENTO 2006 WHEN I HEARD A LOUD BANG. ALL OF A SUDDEN MY CAR STARTED TO BREAK DOWN. THE POWER STEERING WENT OUT, FOLLOWED BY MY BRAKES AND FINALLY, MY CHECK ENGINE LIGHT CAME ON AS THE REST OF THE CAR STARTED TO FALL APART ON THE ROAD. THE CAR COMPLETELY DIED IN THE MIDDLE OF AN INTERSECTION. MY CAR WAS TOWED TO A LOCAL BP WHERE AFTER INSPECTION I WAS INFORMED THAT MY ENGINE CRANK BOLT HAD BLOWN OFF, DESTROYING MY CRANK SHAFT, PISTONS, BELTS, ETC. MY ENGINE IS RUINED AND CANNOT BE FIXED. *TR
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT WHILE DRIVING 30 MPH, THE VEHICLE STALLED. THE CONTACT HAD THE VEHICLE TOWED TO THE DEALER. THE DEALER STATED THAT THE CRANKSHAFT PULLEY BOLT HAD SEIZED IN THE CRANKSHAFT AND HAD BROKEN. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 80,000. THE CONSUMER STATED AS HER DAUGHTER WAS DRIVING, THE CHECK ENGINE LIGHT ILLUMINATED, AND THERE WAS A HORRIBLE NOISE COMING FROM THE ENGINE. THE VEHICLE WAS TAKEN TO THE NEAREST SERVICE CENTER, ONE MILE DOWN THE ROAD FROM HER HOME, BUT THE VEHICLE BECAME MORE DIFFICULT TO STEER AND WHEN HER DAUGHTER PULLED IN THE PARKING LOT, SHE COULD NO LONGER STEER THE VEHICLE AND ALL OF THE INSTRUMENT PANELS LIGHT ILLUMINATED. THE MECHANIC STATED THE REPAIR WOULD REQUIRE THE ENGINE BEING PULLED AND TO REPAIR OR REPLACE THE CRANKSHAFT OR REPLACE THE ENGINE ENTIRELY. EITHER WAY, IT WOULD BE COSTLY. UPDATED 05/19/14 UPDATED 06/10/14*LJ UPDATED 06/13/2014 *JS
SYSTEM WAS IN THE SHOP FOR ROUTINE MAINTENANCE I.E. NEW SPARK PLUGS, DRIVE BELTS, AND SPARK PLUG WIRES. PICKED UP THE VEHICLE AND DROVE FINE FOR A DAY. UPPER CAT CONVERTER GOT CLOGGED... THINGS JUST WENT DOWN HILL FROM THERE. CRANKSHAFT SEAL BUSTED, OIL PUMP FAILED, WATER PUMP HAD TO BE REPLACED. ENGINE RODS STARTED KNOCKING. ENGINE HAS TO BE REBUILT. HAVE BEEN UNABLE TO DRIVE MY SORENTO SINCE MARCH 2013. BOUGHT THE SORENTO IN OCTOBER 2012. JUST HAD THE SORENTO IN THE SHOP FOR ENGINE REBUILD. HAD MONEY SET ASIDE FROM TAX RETURNS. I PAID THE ORIGINAL QUOTED AMOUNT TO HAVE THE REBUILD DONE. IT IS COSTING ME $2000 IN ADDITION TO THE BASE COST THAT WAS ORIGINALLY QUOTED. I DON'T HAVE THAT KIND OF MONEY JUST LAYING AROUND FOR THOSE TYPES OF REPAIRS. OH WELL... GUESS I WON'T BE DRIVING MY CAR FOR ANOTHER WHOLE YEAR. OH... ONE MORE THING.... SINCE I AM THE SECOND OWNER KIA REFUSED TO SERVICE THE VEHICLE WITHOUT THEM WANTING OVER $8000 FOR A NEW MOTOR... FYI.... KIA WARRANTY'S AND BBB ARE BOTH WORTHLESS.. *TR
TL* THE CONTACT OWNS A 2006 KIA SORRENTO. THE CONTACT STATED THAT WHILE DRIVING 50 MPH, THE VEHICLE STALLED AS THE CHECK ENGINE WARNING LAMP ILLUMINATED. THE CONTACT MENTIONED THAT ONCE THE VEHICLE STALLED, HE LOST CONTROL OF THE STEERING WHEEL AND CRASHED INTO A TREE. A POLICE REPORT WAS FILED AND NO INJURIES WERE REPORTED. THE VEHICLE WAS TAKEN TO THE DEALER BUT THE TECHNICIAN WAS UNABLE TO DIAGNOSE THE FAILURE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 106,000.
WIFE WAS DRIVING 40 MPH WHEN THE ENGINE LIGHT AND BRAKE LIGHT CAME ON WITH NO WARNING. THE ENGINE STOPPED AND SHE HAD NO POWER STEERING AND ALSO NO BRAKES. SHE WAS ABLE TO COAST TO A SIDE ROAD AND BARELY GOT THE VEHICLE TO STOP. THE STEERING WAS VERY DIFFICULT. IF IT WOULD HAVE BROKE ANOTHER 200 FEET AHEAD SHE WOULD NOT HAVE BEEN AS LUCKY SINCE THERE IS A VERY SHARP AND DANGEROUS CURVE. THE CURVE HAS A SINGLE GUARD RAIL THAT SHE MORE IN LIKELY WOULD HAVE WENT THROUGH RESULTING IN A 400 FOOT DROP DOWN A STEEP HILL. POSSIBLY RESULTING IN A FATAL CRASH.THE VEHICLE WAS TOWED TO COUGHLIN KIA DEALERSHIP IN NEWARK OHIO. WE WERE INFORMED THAT THE CRANKSHAFT BOLT HAD BROKE IN THE MOTOR. THIS CAUSED THE TIMING PULLING AND MAIN PULLEY TO BREAK OFF. THE RESULT WAS MAJOR ENGINE DAMAGE.THE SERVICE MANAGER CONTACTED HIS KIA REGIONAL REP.AND WAS INFORMED THE DAMAGE WAS NOT COVERED UNDER THE 10 YR./100000 MILE WARRANTY. WE DID HAVE THE SAME DEALERSHIP REPLACE THE TIMING CHAIN 2YRS. EARLIER AT APPR. 57000 MILES AS KIA REQUIRES THIS MAINTENANCE DONE BEFORE 60000 MILES.THEY ALSO REPLACED THE CRANKSHAFT BOLT AS KIA RECOMMENDS IT ALSO. THIS WAS A COST OF NEARLY $800 FOR THIS SERVICE. THE ESTIMATE FOR THE ENGINE REPLACEMENT IS $4000 ON A VEHICLE VALUED AT $6000. KIA REFUSES TO DEAL WITH THIS ISSUE ON THESE MOTORS. THEIR WAS ARECALL ON THE 03 & 04 ENGINES BUT THE PROBLEM STILL EXIST. IT IS JUST A MATTER OF TIME BEFORE SOMEONE WILL BE KILLED DRIVING THESE VEHICLES. *TR
WE ARE THE ORIGINAL OWNERS OF THIS VEHICLE.THE ENGINE SHUTS DOWN-QUITS AT ANY SPEED (EVEN IDLE) LAST TIME AT 60 MILES AN HOUR ON THE FREEWAY. LUCKILY WAS ABLE TO GET TO THE SHOULDER W/O BEING REAR ENDED. THE VEHICLE REFUSED TO START FOR ABOUT 10 MINUTES. THEN I GOT IT STARTED AND RAN ROUGH A COUPLE OF MINUTES THEN CLEARED UP THE REST OF THE WAY. ANOTHER OCCASION THE ENGINE QUIT IN THE MIDDLE OF AN INTERSECTION IN 5:00 TRAFFIC, CAUSING BAD CONJESTION. THE ENGINE LIGHT IS TRIGGERED OCCASIONALLY BUT NO REPAIR CODES ARE SEEN WHEN THE COMPUTER IS HOOKED UP. THIS IS HAPPENING ABOUT EVERY 3 -4 DAYS AND MAYBE 2 X'S IN A DAY. THIS HAS HAPPENED EVER SINCE THE DEALER CHANGED THE TIMING BELT-REGULAR MAINTENENCE ABOUT 80,0000 MI. THE VEHICLE WAS RUNNING AND SOUNDING JUST GREAT BEFORE THE KIA DEALER DID THIS. ON THE WAY HOME, THE VEHICLE WENT DEAD AND HAD NO POWER. GOT THE DEALER TO TAKE IT BACK. THINGS WERE NOT PLUGGED IN--ALTERNATOR ETC. THE MECHANIC WAS IN A HURRY TO LEAVE FOR THE WEEKEND. NOW LEFT LIFTER BANK CLATTERS UPON STARTUP A CODE WAS GIVEN THAT THE DEALER DID NOT CLEAR THE COMPUTER WHEN THE BELT WAS CHANGED. WE CLEARED IT AND THE ENGINE STILL QUITS. THE DEALER WENT OUT OF BUSINESS (GO FIGURE). ALSO THE AIR CONDITIONING QUIT DUE TO A LINE THAT WAS SPLIT POSSIBLY WHEN THE MECHANIC WAS WORKING ON THE TIMING BELT. SOMEONE IS GOING TO GET HURT (ACCIDENT) IF THIS VEHICLE CONTINUES TO DO THIS.NO ONE SEEMS TO KNOW WHAT IS WRONG. *TR
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT WHILE DRIVING 35 MPH, THE BRAKE AND BATTERY LIGHTS ILLUMINATED AS THE VEHICLE STALLED. THE CONTACT WAS ABLE TO RESTART MOMENTS LATER. THE VEHICLE WAS TAKEN TO THE DEALER FOR INSPECTION WHERE THEY STATED THAT A BOLT IN THE CRANK SHAFT WAS FRACTURED AND THE ENGINE WOULD NEED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 99,440. 8/26/13 *CN THE CONSUMER ALSO STATED THE BELTS AND CRANK PULLEY BROKER
FROM 9/2011 TO 7/2013 MY 2006 KIA HAS HAD THIS PROBLEM 3 TIMES AND IS CURRENTLY IN THE SHOP. WHILE DRIVING I HEAR A WEIRD NOISE AND THEN ALL THE DASHBOARD WARNING LIGHTS COME ON AND I LOSE POWER STEERING. WHEN CHECKING UNDER THE HOOD, THE BELTS HAVE ALL FALLEN OFF, A PULLEY IS LAYING UNDER ENGINE AS IS A BOLT. THE LAST TIME THE BOLT HAD BROKEN OFF CAUSING THE PULLEY TO FALL OFF. MECHANIC FOUND THAT THE CRANKSHAFT SPROCKET WAS BROKEN. I'M NOT SURE ABOUT TODAY AS THE CAR IS AT THE SHOP WITH THE BOLT LAYING UNDER THE ENGINE, BUT THE DRIVE PIN THAT GOES INTO THE SPROCKET OF THE PULLEY FELL OUT THE BOTTOM WHEN BEING LIFTED ONTO THE TOW TRUCK. *TR
I WAS DRIVING AND NOTICED THE 4-WHEEL LIGHT CAME ON. I STOPPED THE CAR AND WAITED A FEW MINUTES. WHEN I TURNED THE CAR BACK ON IT WAS MAKING A NOISE. UPON FURTHER INVESTIGATION, I FOUND THE CRANKSHAFT VERY LOOSE. THE CAR IS PRESENTLY AT THE REPAIR GARAGE AWAITING AN ESTIMATE. *TR
MY 22 YEAR OLD DAUGHTER WAS DRIVING THE CAR AT COLLEGE WHEN IT SUDDENLY LOST POWER STEERING AND THEN SHUT DOWN IN TRAFFIC IN THE MIDDLE OF AN INTERSECTION. LUCKILY SHE WAS NOT ON A CURVY ROAD WHEN THE POWER STEERING WENT OUT. WE HAD THE CAR TOWED AND AFTER MECHANIC'S INSPECTION WERE TOLD THAT THE CRANKSHAFT BOLT "WOBBLED" LOOSE AND DISRUPTED THE TIMING BELT ASSEMBLY SHUTTING DOWN THE ENGINE. THIS $2 BOLT HAS CAUSED AN ESTIMATED $3500 REPAIR BILL OR EVEN AN ENGINE REPLACEMENT. OUR RESEARCH HAS UNCOVERED TO US THAT THIS IS A COMMON PROBLEM WITH THIS 3.5L ENGINE. THIS BOLT EITHER BREAKS OR WOBBLES OUT OF IT'S THREADING TO CAUSE TIMING BELT PROBLEMS AND REQUIRES EXTENSIVE AND EXPENSIVE REPAIR TO THE ENGINE. THIS INDICATES TO US A MANUFACTURER'S DESIGN FLAW AND PROBABLE SAFETY ISSUE THAT SHOULD BE ADDRESSED BY KIA WORLDWIDE. *TR
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT WHILE DRIVING 55 MPH, THE MOTOR PULLEY FAILED ON THE ENGINE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE CURRENT AND FAILURE MILEAGE WAS 78,000.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED WHILE TRAVELING 40 MPH THE ALL OF THE WARNING LIGHTS ON THE INSTRUMENT PANEL ILLUMINATED. WHEN THE POWER STEERING MALFUNCTIONED THE BRAKES FAILED TO STOP THE VEHICLE WHEN THEY WERE APPLIED. THE CONTACT MERGED ONTO THE EMERGENCY LANE; HOWEVER, HE WAS ABLE TO CONTINUE DRIVING TO HIS DESTINATION WHERE THE VEHICLE WAS TOWED TO THE DEALER FOR DIAGNOSTIC TESTING. THE DEALER CONFIRMED THAT THE BOLT TO THE HARMONIC BALANCER FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS CONTACTED. THE FAILURE AND CURRENT MILEAGE WERE 59,800. UPDATED 10/02/12*LJ
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED WHILE DRIVING 40 MPH THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO PULL TO THE SIDE OF THE ROAD AND ATTEMPTED TO RESTART THE VEHICLE BUT THE VEHICLE WOULD NOT TURN OVER. THE VEHICLE WAS TOWED TO A LOCAL MECHANIC WHO SUGGESTED THE CONTACT TAKE THE VEHICLE TO AN AUTHORIZED DEALER. THE VEHICLE WAS THEN TOWED TO THE DEALER WHO STATED THAT THE CRANK SHAFT BOLT WAS FRACTURED, AS WELL AS THE PUSH RODS. THE DEALER ADVISED THAT THE ENGINE NEEDED TO BE REPLACED. THE CONTACT DID NOT HAVE THE ENGINE REPLACED. THE FAILURE MILEAGE WAS 46,400.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 30 MPH, THE ENGINE STALLED WITHOUT PRIOR WARNING. THE ENGINE RESTARTED AFTER WAITING A FEW MOMENTS. THE FAILURE OCCURRED TWO TIMES. THE VEHICLE HAD NOT BEEN DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 64,000.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. WHILE DRIVING APPROXIMATELY 30 MPH, THE CONTACT HEARD A CLUNKING NOISE COMING FROM THE FRONT END OF THE VEHICLE. THE CONTACT STATED THAT THE STEERING WHEEL THEN BECAME DIFFICULT TO MANEUVER. THE BRAKE AND CHECK ENGINE LIGHTS ALSO ILLUMINATED ON THE INSTRUMENT PANEL DURING THE FAILURE. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC FOR A DIAGNOSTIC TEST. THE MECHANIC STATED THAT THE CRANK SHAFT BOLT FRACTURED, CAUSING THE CRANK SHAFT PULLEY TO DETACH FROM THE VEHICLE. THE POWER STEERING BELT ALSO BECAME LOOSE AND CAUSED THE POWER STEERING TO FAIL. THERE WAS A VOLUNTARY RECALL FOR THE 2004-2005 KIA SORENTO ADDRESSING THE CRANK SHAFT PULLEY FAILURE. THE MANUFACTURER STATED THAT THE 2006 MODEL WAS NOT INCLUDED IN THE RECALL. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 118,000.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT THE HEADLIGHTS AND REAR LIGHTS HAD TO BE REPLACED AT A MINIMUM OF ONE TIME PER YEAR. THE CONTACT HAD TO CONSTANTLY REPLACE THE BULBS FOR THE LIGHTS BUT THE VEHICLE HAD NOT YET BEEN TO THE DEALER FOR INSPECTION OF THE RECURRING FAILURE. IN ADDITION, THE VEHICLE WOULD STALL SPORADICALLY AND WITHOUT WARNING. THE VEHICLE WAS TAKEN TO THE DEALER WHO STATED TO THE CONTACT THAT THE CRANKSHAFT POSITION SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS UNKNOWN AND THE CURRENT MILEAGE WAS 71,000.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT WAS DRIVING APPROXIMATELY 20 MPH WHEN THERE WAS A SUDDEN LOSS OF POWER WITH THE ILLUMINATION OF THE WARNING INDICATORS ON THE INSTRUMENT PANEL. THE STEERING WHEEL BECAME EXTREMELY DIFFICULT TO MANEUVER. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER FOR DIAGNOSIS WHERE THE TECHNICIAN STATED THAT THE FAILURE WAS CONTRIBUTED TO A DEFECTIVE CRANK SHAFT PULLEY BOLT AND THE ENGINE WOULD NEED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 60,300.
TL* THE CONTACT OWNS A 2006 KIA SORENTO. THE CONTACT STATED THAT ALL THE LIGHTS ILLUMINATED ON THE INSTRUMENT PANEL AS THE VEHICLE STALLED. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS ADVISED THAT THE CRANKSHAFT PULLEY BOLT WAS STRIPPED AND CAUSED THE POWER STEERING BELT TO SPIN ABNORMALLY. THE DEALER ALSO ADVISED THAT THE BOLT COULD NOT BE REPLACED AND THAT THE VEHICLE WOULD NEED A REPLACEMENT ENGINE. THE FAILURE AND THE CURRENT MILEAGE WAS 60,300.
CRANKSHAFT HARMONIC BALANCE BOLT KEEPS BREAKING. BEEN REPLACED 2 TIMES NOW. SAW ON SOME OTHER WEBSITES WHERE OTHER PEOPLE ARE HAVING THE SAME PROBLEM. SOME OF THEM ARE GETTING LAWYERS BECAUSE KIA IS REFUSING TO FIX THE PROBLEM. MY WARRANTY RAN OUT SO THEY WON'T FIX . ALL OF MY REPAIRS HAVE BEEN AT MY OWN EXPENSE. *TR
UNDER NORMAL OPERATION AT HIGHWAY SPEED, THE CRANKSHAFT BOLT BROKE AND ALLOWED THE HARMONIC BALANCER/CRANKSHAFT PULLEY ASSEMBLY TO COME FREE OF THE CRANKSHAFT. THIS RESULTED IN A BROKEN CRANKSHAFT SPROCKET, CRANKSHAFT POSITION SENSOR AND TIMING BELT. THE VEHICLE WAS NOT COVERED UNDER WARRANTEE BECAUSE IT IS NOT CONSIDERED PART OF KIA'S DRIVETRAIN BECAUSE IT IS NOT A LUBRICATED PART. THE VEHICLE WAS OUT OF SERVICE FOR 14 DAYS. ON SEPTEMBER 22, 2011 THE SAME BOLT CAME LOOSE AND SNAPPED THE SPRING PIN ALIGNING THE BALANCER WITH THE CRANKSHAFT SPROCKET. THIS RESULTED IN THE LOSS OF POWER STEERING AND CHARGING SYSTEM WHILE MY WIFE AND DAUGHTERS WERE TRAVELING IN THE VEHICLE. THE VEHICLE WAS NOT UP TO SPEED YET SO THE DAMAGE WAS MINIMAL. THE BOLT HAD TO BE REMOVED AS WELL AS THE BALANCER. THE SPRING PIN HAD TO BE DRILLED OUT OF THE CRANK SPROCKET AND REPLACED.THE VEHICLE WAS OUT OF SERVICE FOR 7 DAYS. *TT
AFTER HEARING A LOUD SCREECHING NOISE FROM MY ENGINE I CALLED THE DEALER & TOLD THEM I WAS COMING IN, MY CAR STALLED ON THE WAY IN. THE DEALER SAID MY CRANK SHAFT PULLEY BOLT BROKE, CAUSING DAMAGE TO MY CRANK SHAFT SENSOR & MY TIMING BELT WHICH I HAD REPLACED A FEW MONTHS BACK. I AM JUST LEARNING THAT THIS IS A VERY COMMON PROBLEM AND THAT KIA IS AWARE OF THIS DEFECTIVE BOLT AND REFUSES TO COVER THE DAMAGE CAUSED TO THE ENGINES WHEN IT BREAKS. *TR
CRANKSHAFT BOLT SHEARED OFF IN MAY 2010 AT 63,000 MILES CAUSING $1200 IN DAMAGE AND TOWING. AFTER HAVING A KIA DEALER FIX THE ISSUE OUT OF MY POCKET BECAUSE I'M A "SECOND OWNER", THE ISSUE HAPPENED AGAIN IN JULY 2011 AT 101,000 MILES. THE DEALER AGAIN HAS TO REPAIR WITH SIMILAR COSTS OUT OF MY POCKET. THIS IS EXTREMELY DANGEROUS AS THE BELT CONNECTING TO THE CRANKSHAFT PULLEY IS ALSO ATTACHED TO THE ALTERNATOR WHICH, WHEN BROKE, CAUSES A LOSS OF ALL POWER, EVEN WHILE THE CAR IS AT FULL DRIVING SPEED. THIS IS ALSO AN EXTREMELY EXPENSIVE ISSUE WHICH AFTER SEVERAL CONVERSATIONS WITH KIA, THEY HAVE YET TO ACKNOWLEDGE IS A PROBLEM. *TR
AUTO LOSING SPEED ON ACCELERATION AND CAR RUNNING POORLY, THEN QUIT COMPLETELY. HAD TOWED TO NEAREST SHOP FOR REPAIR. ALSO HAD TIMING BELT CHANGED AT THE SAME TIME, PER KIAS REQUIRED MAINTENANCE AT 60,000 MI. ON FEB. 18, 2011, REPAIRS WERE MADE: CRANKSHAFT BOLT WAS GONE AND COTTER PIN SHEERED OFF. THESE ITEMS WERE FIXED ALONG W/TIMING BELT REPLACEMENT.. JUNE 15, 2011, CAR LOSING SPEED ON ACCELERATION AND RUNNING VERY BADLY. I WAS ON HIGHWAY. I DID MAKE IT HOME. I HAD AAA COME AND TOW IT TO MY NORMAL REPAIR SHOP, THE DORSCH KIA DEALER. DORSCH OPENED HER UP AND SAID BOLTS WERE NOT TIGHTENED DOWN PROPERLY. MEANTIME, PERFORMANCE AUTO WERE I ORIGINALLY TOOK MY CAR SHOWED ME A BULLETIN ON MY MAKE AND MODEL THAT SHOWED ISSUES WITH THIS BOLT STRETCHING AND COMING OFF AND OR CRACKING OFF. FURTHER, THEY WILL NOT REPLACE ANY PARTS OR LABOR BECAUSE IT IS KIA'S ISSUE THEY SAID. NOW MY CAR IS AT KIA DEALERSHIP AND MY POCKETS ARE EMPTY. *TR
FITTING THAT CONNECTS HOSE TO RADIATOR SNAPPED IN HALF CAUSING COOLANT TO LEAK AND ENGINE TO OVERHEAT. INFORMED BY REPAIR SHOP THAT THIS CAN BE TEMPORARILY FIXED BY INSTALLING A BRASS FITTING USING EPOXY BUT THAT THE ONLY PERMANENT REPAIR IS TO REPLACE THE ENTIRE RADIATOR. *TR
CRANKSHAFT TORQUE BOLT SHEARED OFF CAUSING THE BRAKING AND STEERING TO BECOME STIFF RESULTING IN GREATLY DIMINISHED CONTROL OF THE VEHICLE. THE PULLEY ASSEMBLY BEGAN TO SQUEAL RESULTING IN PARKING THE VEHICLE UNTIL IT WAS TIME TO TAKE IT TO THE DEALERSHIP FOR SERVICE OF THE CONCERN. ENROUTE TO THE DEALERSHIP THE BRAKE AND ENGINE LIGHT APPEARED AND BRAKING BECAME SLUGGISH AND STEERING APPEARED TO BE STIFF. WAS ABLE TO MAKE IT TO THE DEALERSHIP AND I OPENED THE HOOD SEEING THAT THE SERPENTINE BELT HAD COME OFF. THE FOLLOWING DAY THE DEALERSHIP NOTIFIED ME THAT THE CRANKSHAFT TORQUE BOLT HAD SHEARED OFF AND THEY WERE CALLING KIA TO DETERMINE A FIX FOR REPLACING THE BOLT OR IF THE ENGINE WOULD NEED REPLACED. AFTER SOME BRIEF RESEARCH THIS APPEARS TO BE A RECURRING PROBLEM FOR SEVERAL KIA MODELS AND MODEL YEARS. *TR
THE ISSUE IS WITH 2 KIAS I BOUGHT WITHIN THE LAST YEAR. BOTH AUTOMOBILES HAD AIR CONDITIONER COMPRESSORS THAT FAILED WITHIN MONTHS OF ME PURCHASING IT. THE FIRST KIA I BOUGHT WAS A SEDONA 2003. THE SECOND IS A SORENTO 2006 I BOUGHT NOVEMBER 2009. *TR
CAR STALLS WHILE DRIVING WITHOUT ANY WARNING. IT HAS STALLED IN INTERSECTIONS AND JUST RIDING DOWN THE ROAD. WHEN THE VEHICLE STALLS IT JUST CUTS OFF AND MY STEERING WHEEL LOCKS UP AND YOU HAVE NO TIME TO PULL OVER. ALMOST REAR ENDED 3 TIMES IN A WEEK. *TR
2006 SORENTO WAS PURCHASED IN NOV 2005. JAN OF 2006 THE CHECK ENGINE LIGHT CAME ON AND I WAS TOLD IT WAS DUE TO POSSIBLE LOOSE GAS CAP. FIRST TIME TAIL LIGHT WENT OUT WAS IN JULY OF 2006. RIGHT REAR TAIL LIGHT WAS REPLACED. IN OCTOBER OF 2006 A TAIL LIGHT BULB WAS REPLACED DURING MY 15,000 MILE MAINTENANCE. IN NOVEMBER 2006 RIGHT TAIL LIGHT WENT OUT AND KIA REPLACED BULB ONCE AGAIN. IN DECEMBER OF 2006 LEFT TAIL LIGHT WENT OUT AND CHECK ENGINE LIGHT CAME ON. BULB WAS REPLACED AND I WAS TOLD MY SPARK PLUGS WERE MISFIRING AND WERE REPLACED. A DAY LATER MY CHECK ENGINE LIGHT CAME ON AGAIN. I AM NOW TRYING TO SEE WHAT DAY I CAN TAKE OFF OF WORK YET AGAIN TO GO AND HAVE THE CHECK ENGINE LIGHT LOOKED AT. *NM